OK, so Took the boat out for the first test run today, Few things I want to mention not only id this a first run on the engine but last year I had replaced the bellows and all also. But never got to dump it in the water cause I found out about the engine.
So the results are pretty good:
No leaks! (oil or water into the boat)
Temp good!
Oil pressure Great!
Runs strong.
After a while running I noticed some valve noise, So once i got home I adjusted them hot. Before we had done them cold.
I adjusted them while running the engine this time...Made heck of a mess in my bilge. That being said I have a good cleaning I need to do in their. Last time I did it running it wasn't bad really but sense I have the high pressure pump in there, it made a mess this time.
My water pickup hose that goes from the out drive to the gimble came off...easy fix, Turns out then when I tightened the hose clamp down it was on the Hex off the fitting on the out drive and not actually on the hose. lol This time I got it right.
Other then those couple minor issues it ran like a champ. I plan to clean the bilge out and change the oil once before I run it again. Soon hopefully to make sure the valves are in good adjustment.
I messed around the other day a little with the gas struts. ( Jeff I still need to call you) Found out the 40# struts are not enough to hold the hatch up. So I have some 90# to try. But also its not going to be as simple as i hoped. The hinge (on mine at least) will need to be better secured to the bench seat because the gas strut wants to push it, which in turn pushes the whole hatch back not allowing it to close... Also Will need to either do some figuring out about location of the mounts.
Here is a video of the start up at the lunch
CVX-18 Lowrider test run with new engine.